从粗铟熔铸浮渣中回收铟试验研究
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作者单位:

云锡文山锌铟冶炼有限公司, 云南文山 663700

作者简介:

张泽林(1989—),男,本科,主要研究方向为湿法冶金。

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TF843.1

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Experimental Study on Recovery of Indium From Crude Indium Casting Dross
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Yunxi Wenshan Zinc Indium Smelting Co., Ltd., Wenshan 663700 , China

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    摘要:

    粗铟熔铸浮渣中铟主要以三氧化铟、氯氧化铟、氢氧化铟的形式存在,铟含量较高,达到62.64%。本文采用酸浸 -置换-电解工艺回收处理粗铟熔铸浮渣,研究盐酸浸出过程中铟的浸出行为。经Cl-In-H2O系E-pH图分析可知,控制反应pH<2,升高电位,有利于熔铸浮渣中铟化合物的分解。浸出试验结果表明,最佳反应条件为液固比2.0、盐酸浓度7mol/L、反应时间4h、搅拌转速300r/min和反应温度25℃,在此条件下,铟浸出率为52.25%,浸出液中铟浓度可达165g/L。利用铝板进行置换,得到铟纯度约为99.95%的海绵铟,满足电解阳极板质量要求。

    Abstract:

    The indium of crude indium casting slag mainly exists in the form of indium trioxide, indium oxychloride and indium hydroxide. In this paper, acid leaching-replacement-electrolysis process was used to recover and treat crude indium casting slag, and the leaching behavior of indium in hydrochloric acid leaching process was studied.The E-pH diagram analysis of Cl-In-H2O system shows that controlling the reaction pH<2 and increasing the potential are beneficial to the decomposition of indium compounds in the casting slag.The leaching test results show that the optimum reaction conditions are as follows: liquid-solid ratio of 2.0, hydrochloric acid concentration of 7mol/L, reaction time of 4h, stirring speed of 300r/min and reaction temperature of 25℃.Under these conditions, the leaching rate of indium was 52.25%, and the concentration of indium in the leaching solution could reach 165g/L. The sponge indium with purity of 99.95% was obtained by replacement with aluminum plate, which met the quality requirements of electrolytic anode plate.

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张泽林.从粗铟熔铸浮渣中回收铟试验研究[J].绿色矿冶,2024,40(6):67-71,77.

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  • 收稿日期:2024-07-29
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  • 在线发布日期: 2025-11-16
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